306.

When parking the Mustang for the winter at the end of 2010, the bottom end was making some terrible noises. So there it sat until I could scrape together the funds and time to rebuild. Already in the stable was a .030 over block and cheap Summit rebuild kit with hyper pistons, gaskets, etc. I decided to take a break in the gradual GN build and slap together a functional 5.0 and quickly get the thing back on the road. The rotating assembly went out for balancing and was done in no time. My rods had to be resized, which I wasn’t planning on, so the cost was a bit more than I expected, but so be it, the ball was now rolling. The bottom end went together pretty fast and smooth with no real major problems. Upon measuring the piston to deck height, and seeing that the new pistons had 8cc reliefs, I realized that factory .047 headgaskets were going to net me a rather low 8.9:1 compression. My plans are most likely some nitrous in the future, not forced induction, so that was a little low for my taste. Some more careful part selection back when I bought everything would have avoided all this, but I just wanted it to function at this point, not start back from square one with different pistons. Instead I found some Mr Gasket .038 head gaskets which would send it up to 9.1:1 – a little more respectable and higher than the stock 9:1 instead of lower. Good enough.

The old engine came out without much trouble, and my mission was to reuse everything I could and keep money and time spent to a minimum. That doesn’t usually go quite as planned, and this was no exception. I hear the P heads come with some pretty mediocre valve springs, and although I never had any issues, I didn’t really want to chance it now that I was putting in a higher lift Trick Flow cam (this is about the one thing that I splurged on that wasn’t totally necessary.) As luck would have it, I already had a Trick Flow spring kit that was installed on my original E7 heads and had seen very little use. Once the heads were off, a quick inspection showed that some of the valves had a decent amount of carbon buildup and I couldn’t just let that slide. So minus one on the time spent category as I removed and cleaned each valve while swapping valve springs from one head to another (which is kind of a pain with my cheap valvespring compressor) and installing new seals along the way. The guides seemed to be in decent shape, so that helped in the cost department. After that, it was just installing most of the old parts onto the block which didn’t present any real challenges. I had a partial ARP bolt kit, but had to get a few extra items from the hardware store to finish it off.

Here’s where it got interesting. I was looking pretty good on schedule to finish by the first week of September, when I finally hit the snags I’ve come to expect. I decided to upgrade to some Prothane motor mounts (originals were old and shot) and so had to remove the old ones of course. Passenger side, no problem – except for having to dig out the never-used 21mm socket for the oddball 14mm metric nut anyway. Driver side, frozen. Grab the breaker bar, start turning and then the dripping starts. I broke the nut free, but also broke the power steering line in the process. Naturally, none of the 3 auto parts stores (that were open) could get me the line for days, so another setback of time. Ok, I decided, let’s deal with that later and at least get the engine in. With some help, in it goes. When mating it to the trans, however, things were not falling into place. After some thought, I realized that I had forgotten this engine originally was equipped with a manual transmission. So, I’m sure you know where I’m going with this, but the pilot bearing was still in the crank preventing the torque converter from seating in as it should – I had not even thought to check before dropping in the motor. Back out it comes. Then the search for a pilot bearing puller began, which I was not able to get until the next day. So overnight it was dropped into the bay to sit until it could be again hoisted and the bearing could be removed and then dropped back in once again finally.

That is the update until the rest of the little things can be buttoned up, so maybe another week or two at most (busy schedule) and it will be back on the road. Enough to get a little use out of it during the fall, I hope, and then ready for some serious use next summer!

Update: some mid-swap photos.

old engine before teardown

old engine before teardown

enginelesstang

enginelesstang

This entry was posted in 1989 Ford Mustang convertible. Bookmark the permalink.

3 Responses to 306.

  1. wxroz says:

    I think we need an update… and a new photo!

  2. Drivesa5 says:

    …just not very quickly! 🙂

Leave a Reply

Your email address will not be published. Required fields are marked *